Maintenance & Technical > KX500 Original

Timing way out

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skippyhenry:
thanks for the replys, the key is good but the magneto is the wrong one for that year motor.So am going to get a new key way cut into the magneto. Fingers x :-D

Polar-Bus:

--- Quote from: skippyhenry on May 06, 2010, 11:11:27 PM ---thanks for the replys, the key is good but the magneto is the wrong one for that year motor.So am going to get a new key way cut into the magneto. Fingers x :-D

--- End quote ---

This sounds like a recipie for detonation disaster too me....

maddoggy:
i agree with polarbus. i would not take a chance on cutting a new keyway. sounds like a disaster waiting to happen. if you cant afford a new one now, you would be better off to save up for a while and buy the proper mag. seriosly, i wouldn't try the repair. think about what pre-det. does. it fires the fuel/air charge while the piston is still on the way up tries to force it back down. bad, bad, bad things can happen to your motor. motor repairs could cost more than the proper part. not being a jerk here, just trying to help.
                                                                              maddoggy

kaw rider:
you would be money ahead to upgrade to a 90 and newer ignition

Motorrad:
Have you checked it with a degree wheel, and dial indicator down the plug hole?   I wouldn't trust a timing light in this application....

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