Maintenance & Technical > KX500 Original
Kick-backs for dicussion...
paulkx5:
I experienced what I think is the same problem on my 90, when I let off the gas it would pop and there was a power surge, bad enough that the bike would buck pretty hard. In my case this was caused by a rich condition in the carb's idle/ slow circuit. I changed the slow jet from stock to a leaner jet, I can't remember exatly what size though, this completely cured my problem. Might be worth a try. Good luck.
kawdude:
I personally will try anything to make this condition go away. It's annoying as hell.
paulkx5:
kawdude,
I wish I could remember what jet size I ended up with (been over a year), but I think it was a 52 or even a 50. I went through several progressively smaller jets, and the problem kept getting better, and it finally went away with just the jetting change. Hope this helps.
kawdude:
That's ok. Mine currently has a 162 main with a 62 pilot with the clip on the top notch so something definately isn't right. I personally think that it's very rich. Has no go past mid throttle and lots of splooge.
paulkx5:
Ialso had to drop my main jet several steps to get my plug reading correctly. This helped a lot with power and with the splooge.
As far as lacking power above mid throttle, have you checked your KIPS valves to make sure they are timed, and/ or not sticking?
Navigation
[0] Message Index
[#] Next page
[*] Previous page
Go to full version